Dash/Heater/Air Conditioning Project Version 8-8-04

 

1976 GMC ex Palm Beach

Bob Gummersall

Summer 2004

 

A Little Background

 

We have completed the restoration, updating, and refurbishing of our 76 GMC Living area in the fall of 2003.  The project involved removal of all the old Palm Beach yellow and green stuff, headliners, side panels etc.  We left the refrigerator cabinet, bathroom, closet and drawers and the kitchen lower cabinet about the same.  While the coach was gutted, I masked everything, etched, primed and painted out all the cabinets to an off white color.  This included the upper cabinets and front and rear plastic head caps.  The brightness of this off white color made the coach look much larger and open.  We installed new polypropylene sheets to the roof and sides and pumped new expanding foam insulation into the cavities.  We then glued Ozite material on the ceiling and wall paper on the side panels.  We fabricated a new solid surface counter top to accommodate a recessed single sink and recessed two burner stove top with flush tops gave the kitchen a great look while not cooking.  A microwave is under the two burner stove top where the old propane oven was located.  A bed platform in the rear with a new custom quality foam mattress completed the bedroom.  We replaced the faucet and sink stop along with a new raised porcelain toilet to update the bathroom.  A water pump switch was added for convenience.  New carpets over sound and heat barriers provided a base for a new couch and J-lounge in Blue Leather.  Blue Leather drivers and passenger seats along with seat belts made a day of driving a joy.  One-half inch louver blinds provide some privacy all around.

 

       

The chassis components were also restored (rebuilt engine, transmission and 3.42 final drive, re-cored radiator, rebuilt front end, new transmission cooler, disk brakes on the front rear tandems, tires, shocks, etc) to allow us to enjoy some great camping.  We installed a 4KW Honda Generator, 1.5 KW Heart Inverter/Converter/Charger, two 4D AGM Batteries, digital tank monitor and a new master switch panel completed that phase of the project.  Our objective is to restore/rebuild/redesign to make the GMC provide 10 years of motor coaching. 

 

NOW THE NEXT PROBLEM –

 

We knew from having traveled about 7,000 that the stock dash air conditioning system left a lot to be desired.  I had charged it with DuraCool, but there still was just not enough cold air for comfort.  Traveling in August to one rally, we ran the generator and the roof air conditioner, just to get by.  I looked at all the dash modifications that I could find including the add-on evaporator/blower systems used my many GMCers, but all seemed inadequate to really fix the problem.  These add-on evaporator/blower units provide more cool air, but that seems like it would be an appendage and not attractive.  Having driven a couple of hundreds of thousands of miles in other motor coaches, I also felt the GMC driver’s cockpit left lots to be desired from an ergonometric point of view.    I want to be able to adjust the airbag pressure without having to look and bend down to find the control.  I want to adjust the heater/air conditioner or radio without have to bend forward and tanking my eyes off the road for more than a second.  I want to be able to flash my clearance lights communicating with an 18-wheeler without have to reach down and find a knob and pull and push it.  I want to be able to switch to the auxiliary fuel tank without taking my eyes off the road.  My years driving other motor coach and passenger buses gave me the background to design a new instrument display and controls to be safer and easier to use. 

 

SOOOOO- I decided to go for it and install a whole new dash, driver’s cockpit and heater/ac system.  It was not without lots of study and pondering.  I measured and studied the existing heat/ac flow and decided that the best thing for me to do was to buy the components that would have been installed, if my GMC were being manufactured today.  That is the same decision process that led to installing a water-cooled Honda Generator.  I found that Acme Radiator and Air Conditioning has complete high capacity systems that they were providing to Class A motor home manufacturers.  A study of the current components told me that the stock compressor and condenser have plenty of capacity to handle this new larger Acme Evaporator and blower system, so I ordered the pieces for the project.  The technical people at Acme were very helpful with all my questions.

 

 

The new Acme unit and the original control head in the background.

 

So the first step was to remove the old dash and heater/air conditioning system.  This took a couple of hours, since I was not trying to save anything to be reinstalled.  Like most of the 25 year old machines, the screws under the windshield were totally rusted, so I just carefully cut the plastic and removed it piece by piece.  I saved the gauge/control pod which has already been recycled to another GMCer.  A GMCer even want the old control head to use as a training aid.

 

  

 

To remove the old heater/ac system, I first started by bypassing the heater core, connecting the two heater hoses to each other temporarily using the temperature control valve.  I used a catch pan so as to collect the coolant that was in the heater core.  Next all the old wires and vacuum lines were then removed.  The dash control unit was removed and old wires labeled for the installation of the new unit.  The only wires needed were 12vdc, ignition, instrument lights and the wire that goes to the compressor clutch.  The new Acme unit does not need the stock high speed fan circuit that feeds the higher voltage directly from the alternator to the fan through a relay.  So I removed that relay and its associated wiring.  The old red wire that goes directly to the alternator was properly disconnected, labeled and protected because it is butt joined in the wire loom to the main wire that comes to the isolator from the alternator.  The plenum that holds the heater core and the evaporator is held in place with 5 bolts through the aluminum firewall.  Once they were removed, the unit could be pulled out through the opening where the grill was removed.  I had to temporally move the auxiliary transmission cooler to the side to allow space.  It weighs about 40 lbs so care has to exercised, so as to not do damage to the radiator, condenser or anything else that might be in front of the firewall.  This old unit came out with less than 1/16th of an inch clearance between it and the top of the radiator framing.  It took a little tug to get it out.  Once past that frame, it was easy to let it down and out of the grill area.   With all the old stuff removed, you can now start positioning the new Acme components.

 

I did not like having to go inside the glove box, and remove a cover to gain access to the fuses, so I separated the fuses from the connector that goes through the firewall.  This required removing the black tape covering of the wire loom.  It separated nicely, so that I could leave the connector in place and have the fuse panel on a long cord for placement in the new dash so that the access will be easier.

 

 

All the new Acme pieces fit into the space available in the GMC with a little shoe horning.  I had to add a short length of 6” pipe and 2”x14” return air pipe to adapt the Acme unit to the GMC firewall shape.  The rest of the pieces fit.   The Acme defrost registers are shaped to fit through a ¾ inch panel, like in new motor coaches.  This required me to make a template, and cut the flat aluminum right below the windshield in such a way as to have the defrost registers at the right height for the new Dash Top.  I used a high quality jig saw with a metal blade to cut the unusual shape for the new defrost registers.  A little sealant made them air tight.  The defrost hoses have to come from the new Acme Plenum back through the firewall and then up to connect with the registers.  There is room for all this to happen, even above the brake and steering wheel assemblies in the GMC.  The connection between the evaporator/heater chamber and the inside plenum/fan module required that a 6” hole be cut through the firewall. 

 

Plenum/blower mounted inside.

 

Because the Acme is designed for a new motorhome that uses a metal lined 1” plywood firewall, I had to install two ‘stand-off’ elements out of wood, to provide more space between these two units.  I simply glued two wood pieces onto the GMC aluminum firewall spaced to allow the attachment of the plenum/fan module with some wood screws.  This made it necessary to extend the fan inlet to the heat/evaporator module and I used a neopreme sewer coupling from the local hardware store with a clamp to hold it in place.  

 

Like always it takes lots of words to describe what is required, but it is easy to see how this all comes together once you start the process.  All the Acme plastic parts fit fine and were easy to work with.

 

 

 

I now installed the new temperature control valve that is provided by Acme and routed the heater hoses properly.  Again I used a catch pan for the coolant that got away.  The Acme valve is electrically controlled, so the new wiring was routed through the firewall.  Acme provided a cabling loom that would normally have been used in a New Damon Motorhome and I found that it was generous in length and ok to work with.  Besides the wire to the water control valve, a wire needs to go trough the firewall that connects to the evaporator thermostat.  One vacuum line has to be routed to the front of the firewall that controls the outside/inside air valve.  All the vacuum lines are color coded so they were easy to route and install.  I spent some time dressing the vacuum lines and the wiring loom with plastic conduit to make it look nice and protect it from all the vibration of driving this wonderful old machine.

 

I positioned the hot air and cold air registers in the new dash board along with a 2” by 14” hole for the return air register.  This required the fabrication of a rectangular duct about 20” long, that I trimmed as I fitted it into the hole cut in the firewall and butted it to the new Acme Control Head.  I used some adhesive backed door seal material to line this joint so as to provide a mostly sealed joint. 

 

Now I started the testing process.  The heater core was properly connected and I did a cold weather test.  None of the air conditioning elements were connected during this testing.  I started the engine and got some hot coolant circulating through the heater core.  Shut down the engine and refilled the coolant reservoir.  Started the engine again, and tested all the heat and ambient air flow conditions.  Immediately, I was happy with the amount of air flow from all the registers.  So I got hot air from the floor heat registers and hot air out of the defrost registers.  Now I turned the heater demand valve off and got ambient air from all the registers.   I was impressed with the air flow and hopeful for lots of cold air, when the ac functions were checked out.

 

A good friend who is a certified refrigerator technician and I started to test the AC function.   While testing for leaks, we found that the connection at the compressor and the OEM hoses leaked, so we decided to replace the compressor and have new hose assembled.  I decided to stick with R134A refrigerant for lots of reasons that I may enumerate later.  I know that many of you are using the new blends like DuraCool, but I decided to stick with stock stuff.  My buddy recommended adding an accumulator to the system to protect the compressor from damage.  So now with a new compressor, new hoses, new evaporator and expansion valve, new dryer, and a new collector (recommended by my buddy) we are ready to test.  He started by using nitrogen to pressurize the new system.  After hours, it held the 100 psi test and he then used a vacuum pump to pull the system down to -40 psi.  He then added the proper lubricant to the system and charged it with R134a. 

 

The initial testing of the new system showed that the capacity can reduce the ambient temperature about 35 degrees.  This test was done by bypassing the thermostat in the evaporator and the pressure switch so as to test the maximum cooling capability.  In most roof air systems, if you get a reduction of 24 degrees from ambient, the system is working great.  Needless to say, I am extremely happy with this temperature drop.  The real test of this design will be driving this summer in high ambient temperatures and see if we can duplicate the 35 degree drop.   I am satisfied that I now have a modern dash air condition system that has lots of cooling capacity.  I hope that my bride of 48 years is happy on the next trip in hot weather. 

 

Gauges and Controls

 

I am finicky about the driver’s cockpit arrangement and where all the controls are located.  I have lots of experience driving over the road buses, truck, school buses, and motor homes, so I have developed a list of requirements related to the ergonometrics of driving.  The ideal situation is that the driver can activate any control without looking at it, can see every important gauge with a slight glance and can reach every function without moving in the driver’s seat.  That is what I have tried to achieve in with this project.

 

The Control Switches have been relocated to a panel on the left of the driver so that by feel, every function can be located and activated effectively.  It is important to me to be able to know where every switch is located, without having to look down.  For example, I have located separate lighted toggle switches for the head lights and the clearance lights.  These switches actually control 30 amp relays that do the control.  I can, without looking turn off and on the clearance lights without affecting the head lights.  That allows the good neighbor signals between me and truckers on the road.  I can flash on and off the clearance lights without affecting the head lights.  Some people call this the ICC light function.  On my side control panel, I can feel the right and left air bag switches along with the automatic level control switch to control ride height.  I can also feel the Fuel Tank Selector Switch without looking down.  To me, this is very important for safe driving. 

 

 

Recent testing showed air coming out of the four registers at 34 degrees with ambient temperatures in the 80’s.  This was on the highest fan speed and Max A/C, ie all air returned from the cab to be cooled again.  We were traveling at this time and were very comfortable with the fan on the lowest speed with Max A/C and the outlet air was in the 50’s.

 

 

DASH AND INSTRUMENT PANEL CONSTRUCTION

 

It was necessary to construct a new dash and instrument panel to accommodate the new heat/ac hoses and plenum.   Our last coach was a 1999 Monaco Dynasty and I did modification inside that dash board to accommodate new electronics and instrumentation.  I became familiar with how that dash was built and decided to copy it for the GMC.  The design allows all pieces to be removed after they are upholstered to allow access for repair, service and modification.  The result was six major upholstered pieces that interlock with 8 hidden screws and four that are covered with upholstered buttons.  The two side panels are screwed into the existing aluminum channel and held in place on the bottom with downward pressure into the carpet.  The driver’s side panel is wider than the passenger’s to allow control switches.  Fuel tank selector, air bag controls, head and clearance lights, wiper/washer control, control of toad brake, emergency battery connect switch and the switch for the alarm system are placed so that each can be reached by the driver by feel and without having to move in the seat.  I believe this arrangement provides the maximum safety.   To hold the ac registers there is one panel in front of the driver and another in front of the passenger.  This allows maximum cold air flow directed at the people.  These two panels are fastened with blind screws to the side panels and to the firewall.

 

 

There is one center panel with three surfaces that contains the plenum, blower, wiring and hoses.  It is blind screwed into three 1”x1” wood battens that are glued and screwed to the firewall/floor.  It has the cab air return register in the bottom front and two registers for hot air.  This provides the base support for the dash top and instrument panel.  At the driver’s side lower area next to the accelerator, there is a blind door that hides the fuse block.  There is also the cigarette lighter located to power 12vdc devices.

 

The dash top is made of ½” plywood with the cover for the instrument pod permanently fastened.  It is held in place with 3 blind screws and 2 button covered screws that go into the aluminum channel under the windshield glass.  Slot holes are positioned to allow for air flow from the defroster plenums.  The complex shape of the instrument pod cover provided a challenge to upholster.  We end up have to sew only one insert on the side facing the passenger.  Thus the dash cover can be totally removed in a couple of minutes exposing everything inside this area for service.

 

The instrument panels are constructed from the same corian like material that I used on the kitchen counter.  This ¼” sheet material is backed with ¼” plywood.  It has two different pieces that are screwed into the dash cover and frame.  The instruments are gauges that show air bag pressures, vacuum, fuel level, oil pressure, coolant temperature, tachometer and speedometer/odometer.   Alarm status lights for the alternator and brakes are located center left.  The status lights for bright lights, turn signals and toad brake operation are center right.  I used miniature but very bright led lights for this purpose.  Miniatures labels will be added later.

 

 

The second smaller panel houses the radio, ac/heater control, and Digi-panel.  The controls for the radio and ac/heater can be operated without moving in the drives seat or leaning down.  The radio has an infra-red remote that can be held while my hands are on the steering wheel.   This remote control volume and station search functions.

 

The resulting custom dash looks very nice and is in keeping with our restoration/remodeling of our GMC.  My bride can now recline the Flexsteel seat and put her feet on the padded dash like she would a foot rest.  The flat surface also accommodates photographs and flower vases when we get to our destination.

 

 

 

 

Here is the parts list from Acme Air Conditioning

17103 SR 4 East

Goshen, IN 46528

574-534-1516

4215043 Evaporator Kit, Class A Metal $307
4213232 Dash Set, Damon Excaper $296
4102509 5 Black Louvers $41
4100178 50' 2 1/2" Hose $27
4213202 Plenum Kit $146
4570829 Defrost Kit, Triple E $58
Freight to
Seattle $54
Wiring Diagram http://www.acmeair.com/wd4102804rotarywtrvlve.htm
Vacuum Diagram http://www.acmeair.com/vd4102711rotarytauruselewtrvlv.htm


Sales Contact
Wayne Frazier
Tech Contact Terry Van Warmer

 

Other Parts and resources:

New Compressor from
NAPA, can't find the number $150
New Custom Hoses $145

6 yards of Marine grade vinyl

5 yards of ½” high density foam with a glue backing

Two sheets 4x8’ ¼” plywood

One sheet 4x8 ½” plywood

One tube industrial grade polyurethane glue

A Bride that is willing to put up with my antics and sew a section into the dash cover

Lots of staples and some Industrial strength spray on contact cement

Some old arthritic hands and fingers to stretch the vinyl, while operating the staple gun